0 comments Monday, December 28, 2009

Due to earlier delays in our project, the methane system was not sized properly. When we bubble the methane through, only small amount of bubbles can be seen going through the methane capture system. Therefore, we decided to try using cow dung instead of human waste to test the methane system. However, the system still did not show much improvement.

We made our way down to Viknesh Diary Farm and spoke to the owner Mr Manif. He generously allowed us to take a wet sample of the cow dung


Fig1. Methane Capture System, bubbles


Fig2. Cows at Viknesh Diary Farm


Fig3. Cow that gave us its dung


Fig4. Jian Wei, Elijah and Mr Manif

0 comments Wednesday, December 23, 2009

Last week of planting


Fig1.Week 4. Commercial

0 comments Monday, December 14, 2009

Second last week of planting.


Fig1. Week 4. Prototype run 2


Fig2. Week 3. Commercial fertilizer

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Once the metal prototype was in place, we started the first run. This prototype was left running for 16 in total. 10 days anaerobic run and a 6 days aerobic run before we took the samples for testing. This second run was a lot smoother than our first run. By now, we have the necessary experience to conduct the experiment smoothly. The entire loading process went on without much of a hiccup.


Fig1. Preparing for the prototype run


Fig2. Loading the sludge into the digester


Fig3. Clearing the surrounding area



Fig4. Using water to rinse the system and surrounding

Following this, the gas test was conducted after ten days and these are the results obtained.



Fig5. Carbon dioxide drager tube reflecting a small amount of carbon dioxide present



Fig6. Hydrogen sulfide drager tube reflecting a hge amount of hydrogen sulfide (more than 60ppm)



Fig7. Methane drager tube shows slight color change, indicating presence of methane

Following the gas testing, we took a sample and headed down to Ensure Engineering's lab to conduct further test regarding the components in the digested sludge. The results are reflected in the final report.

0 comments Friday, December 4, 2009

Still some more planting


Fig1. Week 4. Prototype run 1


Fig 2. Week 3. Prototype run 2


Fig3. Week 2. Commercial

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After the destruction of the original prototype and with all the leaking problems, we decided to change our material of construction and use metal instead. The metal would be welded together and would hence eliminate the problem of leaking. Moreover, the metal would definitely be able to withstand the 60oC of heating brought about at the aerobic stage.

The metal used was taken from an old cabinet and some of the valves and pipes were re-used from the old prototype. The air pump and the heater was dismantled and re-used.

The metal prototype was completed in about a week.


Fig1. Using scrap metal, our prototype was built


Fig2. The top of our metal prototype


Fig3. The separating portion between the two stages



Fig4. The completed prototype at SVF

Due to the burnt prototype, our aerobic digestion stage was being unroutinely interrupted. We did the next best thing by salvaging the remains of the aerobic stage, use a water bath as a heating component and use another pump to perform the bubbling as a form of mixing. This process was done for an hour before we tested the aerobic mixture.


                     Fig5. Air Pump                                             

Fig6. Aerobic sludge solution in the water bath

0 comments Wednesday, November 25, 2009

Our fourth week of planting



Fig1. Week 4. Actual digester


Fig 2. Actual digester


Fig 3. Week 2. Prototype run 1


Fig4. Week 2. Prototype week 2


Fig5. Week.1 Commerical